Industrial Driveway Crossing Repair
The Job
This industrial driveway crossing repair project is located in Frederick, Maryland. MARC’s Brunswick Line’s Frederick extension passes through multiple industrial sites & driveways. This particular crossing served as the driveway of a ready mix concrete operation, so saw extensive high dynamic loading in a wet environment.
The Challenge
The repair had to be performed without disrupting either rail or industrial traffic. There was a four-hour window between the last morning train and the first evening train for performing the repair to the eight modular tub crossing panels. The settlement was up to two inches, with extensive spalling.
The Solution
CJGeo’s crew installed supplemental bolts due to replace the OEM center panel anchors, and then grouted the crossing in the mid-day window, without disruption to any stakeholder. The structural polymer grouting work took less than a day onsite. The work was done between the morning and evening commuter trains, but multiple freight trains used the crossing during the repair.
CJGrout 48NHL was the grout of choice. CJGrout 48NHL is formulated specifically for high, dynamic loading environments, such as rail crossings, and airfields. It provides superior bearing capacity, excellent resiliency to dynamic loads, and is great for correcting differential settlement between panels. Because it is relatively low mobility, CJGrout 48NHL is unlikely to affect adjacent pavement.
Speak With An Expert
Facing a similar challenge to this industrial driveway crossing repair project? Give us a shout or shoot us a text. Click the state marker for the location of your project for contact info for the appropriate rep.
Mine Shaft Abandonment
The Job
This mine shaft abandonment project is located in an area with a significant number of abandoned coal mines. The inverted pyramid concrete cap on a Civil War-era coal mine shaft collapsed catastrophically. The mine shaft was located in the middle of a suburban golf course in Richmond, Virginia. The collapse was due to the deterioration of timbers lining the shaft through soft sandy soils. The soft sandy soils extended approximately 25VF down to rock. As the timbers deteriorated with time, they lost the ability to support the cap.
The Challenge
The tunnel shaft was completely full of water, which was approximately 60 degrees. The area around the cap was very unstable and did not facilitate top-down access over the mine shaft.
The Solution
The repair was designed around drilling well casing at an angle to intercept the mine shaft at various elevations between the bottom of the cap and socketed down into the underlying rock. 3.5PCF hydro insensitive polyurethane grout was chosen for its ability to provide the necessary structural support to the cap.
CJGeo performed pre-mobilization testing at our facility in collaboration with the design engineer to ensure that the grout would perform as desired. CJGeo placed CJGrout 35NHV geotechnical polyurethane through approximately 15 different injection points, grouting from the top down. The end result was a plug extending at least 5′ into the shaft through rock. This plug ensures that the shaft through soft soils is completely stable.
Speak With An Expert
Facing a similar challenge to this mine shaft abandonment project? Give us a shout or shoot us a text. Click the state marker for the location of your project for contact info for the appropriate rep.